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N313WB Restoration

December 12, 1993
Total Time transferred from navy records. TT is 11,106.0 hours. 0.0 hours SMOH
Aircraft Major Overhaul This Date-

Aircraft completely disassembled and paint stripped. All wiring, control, hydraulic, oxygen and armament systems removed.  Aircraft inspected for damage and corrosion.  Fuselage assembly repaired and re-skinned as required.  Inboard wing panels replaced with NEW assemblies.  Outboard wing panels overhauled.  All critical components N.D.T inspected and painted or re-plated.  All hardware N.D.T. inspected and plated or replaced. Wing and fuselage mating lugs N.D.T. inspected.  Left wing flaps, horizontal and vertical stabilizers overhauled.  Ailerons, right hand wing flaps, rudder, elevators and landing gear doors replaced with NEW assemblies.  All flight controls painted and balanced.  All fairings replaced or overhauled.  All control cable assemblies, bearings and rod ends replaced.  Interior of wings and fuselage painted.  All hydraulic components overhauled.  All NEW hydraulic tube assemblies fabricated and installed.  All flexible hose assemblies replaced.  Aircraft re-wired.  Aircraft assembled complete.  Fuel cells overhauled and installed.  Landing gears overhauled and re-installed.  Cockpit heater overhauled and tested satisfactory.  NEW instrument panels fabricated and installed with NEW or O.H.C. instruments.  All cockpit controls overhauled, complete and installed.  Oxygen system overhauled and installed. O2 and N2 bottles hydrostatic tested.  Systems tested and function test satisfactory.  All electrical components replaced or overhauled.  NEW canopy, glass, tires, nosewheel assembly, battery, aileron seals, ELT, fabric components, and seat harness assembly installed.  Engine cowlings and cowl flap drive system overhauled.  Aircraft exterior painted.  Complete A.C. static inverter system installed.  Radio package installed consisting of dual KX155s, KMA 24H. KN G4, KLN 88 and WXIO.  PN101 and S-TEC 60-2 Autopilot installed, rigged and function tested.  Goodrich wheels and brakes, fire suppression system, standby hydraulic system, engine pre-oil and scavenge systems installed.  Aircraft given a dimensional and symmetry check.  Aircraft weighed and new weight and balance report compiled.  Compass swung and correction card installed. Aircraft inspected, repaired, assembled and rigged I.A.W. Navair OZA-35, GH-4, OI-60 FGB-7, OI-60 FGB-503 and OI-60 FGB-6,NAVAER OZA-35 GH-502, NAVWEDS OI-60 FGB-2 and OI60 FGB-4, T.Os 1T28 A-6, 1 T28 B-2, 4 and 1-74-3, 4 and 2-60-3, 4and A2-3-4, FAR Part 43 and AC43-13.

“I certify that this aircraft has been inspected on 12 December 1993 I.A.W. the scope and detail of a major inspection as detailed in the aircraft’s approved inspection program.  I have found that it is in a condition for safe operation.”

-See N.D.T. plating, materials certificates and maintenance release tags.

- See Engine Logbook- See Propeller Logbook- See Weight and Balance and Loading Graphs

-A.D. Compliance correct through this date.

-Experimental Operating Limitations issued.

 313WB Log 011110.jpg

 

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